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On February 13, 2018, around noon local time, a Boeing 777-222 [a] operating as United Airlines Flight 1175 (UA1175), experienced an in-flight separation of a fan blade in the No. 2 (right) engine while over the Pacific Ocean en route from San Francisco International Airport to the Daniel K. Inouye International Airport, Honolulu, Hawaii. [1]
The US National Transportation Safety Board investigated the accident. [9] The final report cited pilot error, determining pilot Coleman Dodd was flying too low. Investigators said a low therapeutic amount of an antihistamine was found in his blood but could not say with certainty it contributed to his inability to avoid crashing. [10]
The United States National Transportation Safety Board, which had also assisted in the Flight 185 investigation, told the NTSC that the cause of the crash was a suicide by pilot (in this case the captain) via a letter sent on 11 December the same year. [4] [5]
WASHINGTON (Reuters) -The National Transportation Safety Board on Thursday cited United Airlines crew failure in a December 2022 flight that sharply lost altitude before recovering shortly after ...
The National Transportation Safety Board (NTSB) is an independent U.S. government investigative agency responsible for civil transportation accident investigation.In this role, the NTSB investigates and reports on aviation accidents and incidents, certain types of highway crashes, ship and marine accidents, pipeline incidents, bridge failures, and railroad accidents. [3]
The National Transportation Safety Board has issued an urgent warning to airlines that fly the Boeing 737, saying a failure first seen on a United Airlines flight in February could cause problems ...
13 February 2018, United Airlines Flight 1175 A PW4077 fan blade failure caused significant engine damage to a Boeing 777-200 on descent into Honolulu from San Francisco. [14] Routine fan blade inspection in 2005 and 2010 had shown a crack in the blade's metal structure but insufficiently trained inspectors had confused it for a defect in the ...
On June 28, 1998, United Airlines Flight 863, a Boeing 747-400 flying United's regularly scheduled transpacific service from San Francisco International Airport to Sydney Airport was forced to shut down one of its right-wing engines and nearly collided with San Bruno Mountain while recovering from the engine failure.